Real removed the existing tubing from the well and re-entered the lower diversion assemblies with a small drill to mechanically remove a blockage in the tubing string.
The company said Monday that the well had been completed with a production tubing string and the post-frack flow back operations had resumed, which is expected to take several days.
It added the well was flowing back the frack fluids at a rate of roughly 300 barrels per day with reported increasing gas influx.
Real